Acronyms
anticipated
transient
without
scram
(ATWS)
Auxiliary
Feedwater
Pumps
(AFWPs)
Code
of
Federal
Regulations
(CFR)
Commonwealth
Edison
(ComEd)
Condensate
Storage
Tank
(CST)
Electric
Power
Research
Institute
(EPRI)
Final
Safety
Analysis
Report
(FSAR)
Idaho
National
Engineering
Laboratory
(INEL)
local
leak
rate
testing
(LLRT)
loss
of
coolant
accidents
(LOCAs)
Nuclear
Steam
Supply
System
(NSSS)
Pressurized
Water
Reactors
(PWRs)
shortened
version
of
RELAPSE
(RELAP)
Reactor
Leak
&
Power
Safety
Excursion
code
(RELAPSE)
three-dimensional
(3-D)
To
Find
Almost
Any
Acronym
for
Science
and
Technology
see
EDA
Master
Acronym
List.
Most
Recent
Work
Commonwealth
Edison,
BWROG, EXELON
and
others
(10/96
to
Present)
Mr. Miller provided an
evaluation used EPRI mythology for GL 96-06 and applied it to the Reactor
Containment Fan Cooler (RCFC) system for Byron and Braidwood. The
column closure waterhammer event was assessed. The calculation
required the determination of the voiding in the RCFC piping, the pump and
piping characteristics of the system, the sonic velocities in the piping,
the column closure velocity, waterhammer transmission coefficients and
pressure clipping and cushioning values. Theses values were used to predict
water hammer loads in the piping and to compare these loads to loads that
were calculated using other methods.
Mr.
Miller
provided
RELAP5/MOD3.3
training
to
ten
Exelon
engineers
at
the
Braidwood
Stations.
The
engineers
were
from
different
geographical
areas
of
the
Exelon
Corporation.
The
training
was
given
in
three
different
levels,
Introduction
to
RELAP5
Application,
Intermediate
RELAP5
Application
and
Advanced
RELAP5
Application.
The
participants
gain
a
working
knowledge
of
using
XMGR
and
developing
RELAP5
models
of
plant
problems
and
solving
the
problems
using
RELAP5.
A
working
knowledge
of
Controllers,
heat
transfer,
heat
exchangers
and
pumps
was
also
demonstrated
with
many
in
class
examples.
Mr.
Miller
began
his
consulting
work
at
Commonwealth
Edison
by
evaluating
a
long-standing
problem
for
the
Auxiliary
Feedwater
Pumps
(AFWPs)
for
Byron
Units
1
&
2
and
Braidwood
Units
1
&
2.
Both
of
these
plants
are
Westinghouse
Pressurized
Water
Reactors
(PWRs)
with
large
dry
containments.
Since
the
beginning
of
plant
operation,
a
very
low-pressure
signal
in
the
pump
suction , which occurred during
the
start
of
the
AFWPs, caused
spurious
alarms
and/or
trips.
Mr.
Miller
modeled
the
AFW
piping
system
from
the
Condensate
Storage
Tank
(CST)
to
the
Steam
Generators
using
the
computer
program
RELAP5. RELAP5 requires flow
loss coefficients and other characteristics of the the system to be
modeled. With
this
model
he
was
able
to
assess
the
root
cause
of
the
problem
and
propose
a
modification
to
correct
it.
Once
the
modification
was
implemented,
the trip problem
was
eliminated.
This
effort
required
Mr.
Miller
to
walk
down
the
systems
and
coordinate
information
from
the
site
System
Engineers.
Mr.
Miller
attended meetings
with
plant
staff
to
discuss
results
and
to
evaluate
alternatives.
Another
project
that
Mr.
Miller
completed
was
the
evaluation
of
three-dimensional
effects
on
the
steam
generator
internals
due
to
pipeline
break
depressurization
wave.
When
a
steam
line
leaving
the
steam
generator
is
assumed
to
rupture,
large
forces
are
created
in
the
steam
generator
because
of
the
flow
out
the
break.
As
part
of
the
evaluation
of
steam
generator's
structural
integrity
evaluation,
Commonwealth
Edison
performed
a
dynamic
one-dimensional
analysis
of
the
steam
generator's
internal
structure
subsequent
to
the
rupture
of
the
steam
line.
During
the
review
of
licensing
amendments
for
the
Steam
Generator
replacement
project
for
Byron
and
Braidwood,
the
NRC
questioned
what
would
three-dimensional
flow
effects
have
on
the
Steam
Generator
structure?
Using
a
multi-stream
tubes
calculation
with
two-phase
flow
characteristics
being
modeled,
Mr.
Miller
evaluated
the
three-dimensional
effects
of
the
flow
stream
and
provided
a
response
to
the
Nuclear
Regulatory
Commission.
This
response
was
accepted
and
no
further
action
was
required.
Mr.
Miller
participated
in
the
first
reload
evaluation
using
the
Replacement
Steam
Generators
provided
by
Babcock
&
Wilcox
for
Braidwood
and
Byron
Nuclear
Power
Stations.
Since
an
expedited
schedule
was
required
to
successfully
complete
the
reload
safety
analysis,
Mr.
Miller
was
asked
to
maintain
a
residence
at
Westinghouse
in
Pittsburgh
to
support
the
Vendor
in
completing
the
reload
safety
analyses
on
schedule.
Mr.
Miller
developed
input
for
use
in
the
thermal
hydraulic
computer
program,
NOTHRUMP,
and
evaluated
the
feedwater
transient
for
the
reload
safety
analysis.
To
complete
this
project,
Mr.
Miller
worked
with
other
members
of
the
Westinghouse
safety
analysis
team
and
used
Westinghouse
software.
All
analyses
were
completed
on
schedule
and
within
budget.
Mr.
Miller
completed
an
evaluation
of
local
leak
rate
testing
requirements
to
determine
if
Commonwealth
Edition
could
request
an
exemption
to
some
of
their
local
leak
rate
testing
(LLRT).
A
steam
leak
model
was
developed
that
matched
the
test
data
within
10
per
cent.
The
computer
program
was
used
to
predict
the
depressurization
rate
of
the
steam
generator
after
it
was
isolated.
A
computer
program
was
used
to
model
a
spectrum
of
small
breaks
to
determine
the
break
flow
into
the
containment
for
different
size
breaks
and
GOTHIC
was
used
to
predict
the
pressure
and
temperature
response
in
the
containment
due
to
these
small
breaks.
Mr.
Miller
completed
all
these
analyses
and
developed
a
response
matrix
for
leak
detection
requirements.
Mr.
Miller
successfully
completed
the
technical
specification
changes
for
Condensate
Storage
Tank
level
requirements
and
AFWP
actuation
set
point
levels.
Mr.
Miller
also
performed
an
evaluation
for
the
adequacy
of
vortex
correlations.
A
correlation
was
developed
and
proposed
that
provided
adequate
protection
from
the
formation
of
air
ingestion
vortices.
Mr.
Miller
supported
the
plants
by
providing
heat
exchanger
calculations
and
natural
circulation
calculations
for
the
plants
during
shutdown.
Mr.
Miller
also
assisted
plant
engineers
in
taking
measurements
and
assessing
problems.
This
information
was
used
to
predict
the
temperatures
and
flows
in
the
reactor
cavity
during
shutdown.
Mr.
Miller
has
developed
corporate
web
sites
for
several
companies.
The
development
of
these
web
sites
included
the
technical
and
administration
of
the
web
site
and
the
active
top
10
indexing
of
the
corporate
sites
on
the
major
search
and
directory
services.
Mr.
Miller
is
currently
developing
intranet
and
web
security
for
windows
2000
platforms
for
two
companies.
The
internet
security
will
allow
outside
clients
and
employees
to
access
confidential
documents.
back
to
top
Other
Work
Related
to
Plant
Design, Maintenace and
Construction
Plant
Design
As
an
Engineer
at
Black
&
Veatch
and
at
River
Bend
Station,
Mr.
Miller
was
responsible
for
the
proper
design
and
redesign
of
various
systems.
As
a
Senior
System
Engineer,
Mr.
Miller
was
responsible
for
ensuring
that
the
designs
were
installed
properly
and
that
systems
were
redesigned
correctly.
During
the
final
construction
of
River
Bend
Station,
Mr.
Miller
worked
in
the
field
to
ensure
the
design
drawings
were
followed
and
the
tested
system
functioned
according
to
specifications.
When
a
system
was
not
functioning
according
to
design
specifications,
Mr.
Miller
developed
a
root
cause
evaluation
to
determine
the
reason
for
the
problem.
Once
the
root
cause
was
determined,
a
design
change
was
developed
and
implemented
as
a
modification
package.
The
modification
package
contained
the
root
cause
evaluation,
design
specifications,
new
safety
analyses
(if
required),
the
electrical
design
evaluation,
the
civil/structural
design
evaluation,
the
mechanical/system
design
evaluation,
and
the
integrated
design
package.
The
modification
package
also
contained
the
safety
evaluation
(i.e.,
10
CFR
50.59
for
nuclear
power
plants),
the
environmental
impact
evaluation,
Final
Safety
Analysis
Report
(FSAR)
changes
and
procedure
changes.
All
modification
packages
contain
retest
requirements
and
construction
procedures.
Mr.
Miller
worked
closely
with
Maintenance
and
System
Engineers
to
ensure
that
the
new
designs
were
constructed
and
tested
properly.
Mr.
Miller
was
responsible
for
the
modification
package
and
all
quality
assurance
associated
with
the
modification
on
a
particular
system.
He
had
system
design
responsibility
for
7
major
systems.
When
Mr.
Miller
was
promoted
to
Director
of
Engineering,
he
was
responsible
for
all
Nuclear
Steam
Supply
System
(NSSS)
components.
There
were
about
100
NSSS
components
and
most
of
these
were
systems.
Many
critical
modifications
were
made
to
improve
the
reliability
of
the
station.
At
Black
and
Veatch,
Mr.
Miller
was
project
engineer.
One
of
his
projects
was
to
modify
ASME
B31.1
and
ASME
III
piping,
which
contained
the
safety
relief
valves
for
the
primary
system.
All
work
was
reviewed
by
the
Nuclear
Regulatory
Commission
and
was
approved
by
them.
This
work
required
knowledge
of
the
ASME
codes
and
computer
programs
used
to
evaluate
the
design.
All
system
design
work
completed
at
Black
&
Veatch
required
a
System
Analysis.
The
System
Analysis
developed
several
alternatives
to
provide
a
specific
system
function
and/or
solution
to
a
problem.
Pros
and
cons
for
each
of
these
alternatives
were
developed
and
a
cost
evaluation
was
performed
for
each
alternative.
From
the
System
Analysis,
the
final
recommendation
for
a
system
design
was
provided,
which
also
contained
construction
specifications
and
preliminary
drawings.
Design
and
construction
drawings
were
provided
through
the
aid
of
a
computer.
At
Black
and
Veatch,
Mr.
Miller
designed
several
fire
protection
systems
for
coal
burning
plants.
Design
and
construction
drawings
and
design
specifications
were
developed.
He
also
help
design
a
solar
power
site
for
Electric
Power
Research
Institute
(EPRI).
back
to
top
Maintenance
At
River Bend Station (1000 MW BWR), I was the project design manager on numerous
modifications. I worked with the Maintenance and operation department
to trouble shoot problems, schedule the work and implement the design and
construction activities. Used pert and scheduling software to
schedule the projects. I was also responsible for allocating money
and for oversight to construction crews.
back
to
top
Construction
Work
Mr.
Miller
has
worked
on
several
construction
projects
while
he
was
going
to
school.
These
included
working
as
a
construction
laborer
during
the
construction
of
a
5-story
silo
bin
in
Dardanelle,
Arkansas
and
on
the
construction
of
a
water
purification
facility
in
Dover,
Arkansas.
Mr.
Miller
grew
up
on
a
ranch
and
dairy
farm
where
many
small
construction
projects
were
designed
and
constructed.
While
Mr.
Miller
worked
at
Arkansas
Power
and
Light
as
an
Instrument
Repairman,
he
supported
the
operation
of
three
gas
and
oil
fired
boilers.
This
responsibility
also
included
some
design
changes
and
over
seeing
the
performance
of
the
plant
chemistry.
Overall,
Mr.
Miller
has
been
involved
in
many
construction
projects
and
he
understands
what
it
takes
to
successfully
finish
them.
While
at
the
power
station,
Mr.
Miller
was
responsible
for
many
construction
projects
that
he
designed.
He
followed
through
on
these
projects
until
they
were
successfully
tested,
implemented
and
operational.
back
to
top
Safety
Analysis
At
NUS
Corp.,
Mr.
Miller
developed
models
for
containment
pressurization
and
heat-up.
He
also
developed
models
to
simulated
reactor
behavior
during
loss
of
coolant
accidents
(LOCAs)
and
for
analyzing
anticipated
transient
without
scram
(ATWS)
events.
In
addition,
many
other
thermal-hydraulic
related
analyses,
such
transient
and
steady
state
fluid
flow
events,
were
performed.
At
the
Idaho
National
Engineering
Laboratory
(INEL),
Mr.
Miller
worked
in
the
code
verification
and
model
development
groups.
He
developed
input
models
for
RELAP4
and
FRAP
(a
fuel
rod
simulator)
and
supported
code
development
efforts.
At
Black
&
Veatch,
Mr.
Miller
was
responsible
for
developing
all
computer
programs
used
to
perform
safety
analyses
for
the
nuclear
projects.
At
River
Bend
Station,
Mr.
Miller
served
in
several
different
capacities
that
included
the
development
of
the
ATWS
model
for
boron
injection,
computer
quality
assurance
for
safety
related
programs,
and
the
development
of
computer
codes
and
programs
used
to
perform
engineering
analyses
on
site.
Mr.
Miller
also
served
as
a
senior
technical
advisor
and
technical
director
on
all
nuclear
fuel
and
thermal-hydraulic
reactor
design
and
analysis
issues.
At
Scientech,
Mr.
Miller
provided
senior
technical
engineering
support
and
guidance
on
many
technical
issues
and
work
assignments
that
were
performed
by
in-house
staff
and
by
the
Nuclear
Regulator
Commission’s
research
and
regulatory
staff.
As
the
President
and
Principle
Engineer
of
EDA,
Incorporated,
Mr.
Miller
provided
technical
consulting
and
Engineering
on
a
number
of
issues
related
to
reactor
thermal
hydraulic
design
and
analysis
for
Commonwealth
Edison
corporate
and
field
engineering
and
for
the
Boiling
Water
Owners
Group
(BWROG).
To
develop
the
probabilistic
risk
analysis
(PSA)
for
the
power
plant,
precise
system
models
of
the
plant
were
constructed
using
system
specifications,
plant
drawings,
plant
walk
downs,
operator
interviews
and
detailed
analysis
using
CAFTA
and
MAAP.
The
CAFTA
and
MAAP
computer
programs
were
used
to
develop
accident
scenarios,
event
trees
and
fault
trees.
In
addition
to
the
nuclear
steam
supply
systems
(NSSSs)
and
balance
of
plant
(BOP)
systems,
the
containment
systems
were
also
simulated
in
the
CAFTA
analyses
to
predict
the
containment
failure
frequency.
The
models
were
also
modified
to
include
fire
risk.
From
this
information,
maintenance
and
outage
activities
were
prioritized
and
safety
assessments
were
performed
for
special
events
and
evolutions.
The
River
Bend
PSA
was
submitted
to
the
NRC
as
the
station’s
individual
plant
examination
(IPE).
An
example
for
using
the
IPE
is
presented
in
the
following
paragraph.
The
power
plant
was
to
start-up
from
an
outage
when
one
of
the
two
main
transformers
failed.
Since
the
transformers
were
not
in
the
Technical
Specification,
they
were
not
considered
a
safety
threat
to
the
plant.
The
Senior
Vice
President,
in
trying
to
be
thorough,
still
required
an
IPE
to
ensure
that
their
start-up
was
safe.
The
transformers
were
not
in
the
IPE
model
so
they
were
modeled
and
included
in
the
IPE
model
and
then
risk
change
probabilities
were
determined.
As
it
turned
out,
having
one
transformer
out
when
the
plant
started-up
was
risk
significant
and
plant
staff
were
informed
of
the
finding.
The
utility
was
losing
$350,000
per
day
while
the
plant
was
down,
and
plant
staff
was
anxious
to
start-up.
It
was
imperative
that
a
good
explanation
of
the
IPE
process
was
presented.
Mr.
Miller
developed
a
presentation
that
explained
in
layman
terminology
the
safety
risk
of
starting
the
plant
with
only
one
transformer
available.
There
was
a
very
robust
interchange
of
information
at
the
meeting,
but
by
the
end
of
the
day
it
was
concluded
that
it
was
risky
to
start-up
the
plant
without
the
additional
transformer.
The
plant
stayed
down
for
an
additional
three
days
so
a
new
transformer
could
be
installed.
This
was
an
extremely
beneficial
use
of
the
IPE
since
it
kept
plant
staff
from
putting
the
plant
at
risk.
Mr.
Miller
was
responsible
for
developing
and
implementing
a
plan
to
allow
the
BWRs
to
take
the
Shut
Down
Cooling
(SDC)
or
Residual
Heat
Removal
(RHR)
heat
exchangers
out
of
services
during
the
refueling
of
the
reactor.
Fuel
Pool
Cooling
was
to
be
exclusively
used
to
cool
the
fuel
pool
and
reactor
cavity.
Since
the
suction
and
discharge
piping
for
fuel
pool
cooling
was
located
at
the
top
of
the
fuel
pool,
natural
circulation
through
the
reactor
core
had
to
be
established
to
ensure
adequate
cooling
of
the
fuel.
Detailed
heat
exchanger
models
were
developed
to
perform
with
RELAP5
to
calculate
the
natural
circulation
flow
rate
through
the
core
and
to
establish
when
the
SDC
could
be
taken
out
of
service.
Prior
to
the
shutdown
of
the
first
unit,
a
testing
plan
was
prepared
that
ensured
proper
measurement
of
the
water
temperature
in
different
locations
throughout
the
facility
was
achieved.
The
validation
of
the
analytical
models
was
demonstrated
by
the
successful
use
of
natural
circulation
cooling
in
the
outage.
back
to
top
Computer
Program
Development
and
Use
At
NUS
Corporation
in
Gaithersburg,
Maryland,
Mr.
Miller
was
responsible
for
performing
the
first
containment
analysis
work
for
the
South
Texas
Project.
RELAP3
was
the
computer
program
of
choice
in
performing
subcompartment
pressurization
and
heat-up
analyses
and
CONTEMP-LT
was
the
program
used
to
simulate
pressurization
and
heat
up
in
the
large
dry
containments.
Models
were
developed
for
each
configuration.
Modifications
to
the
input
were
necessary
to
satisfactorily
model
the
compressibility
of
steam
in
RELAP3.
Mr.
Miller
also
made
modifications
to
CONTEMPT-LT
source
coding
to
include
a
subroutine
that
would
simulate
fires.
Additionally,
Mr.
Miller
used
RELAP3B
to
simulate
an
anticipated
transient
without
scram
(ATWS)
of
the
San
Onofre
Reactor.
Other
example
analyses
that
Mr.
Miller
performed
were
as
follows.
Mr.
Miller
wrote
a
program
that
simulated
the
dynamic
change
in
a
tank
with
several
different
flow
streams
entering
and
exiting.
Mr.
Miller
also
wrote
a
program
that
determined
the
concentration
level
of
hydrogen
gas
and
several
gases
when
hydrogen
is
being
released
into
the
a
large
containment
where
a
hydrogen
recombiner
was
operating.
In
1977,
Mr.
Miller
moved
to
Idaho
Falls
to
take
the
position
as
Senior
Engineer
in
Code
Verification
and
Development
at
the
Idaho
National
Engineering
Laboratory
(INEL).
His
immediate
supervisors
were
Tom
Charlton
and
Dick
Rice.
The
laboratory
was
operating
the
Loss
of
Fluid
Test
(LOFT)
facility,
Semi-scale
and
monitoring
the
testing
at
the
Two
Loop
Test
Apparatus
(TLTA)
located
at
General
Electric
in
San
Jose,
California.
His
first
assignment
was
to
develop
an
input
deck
for
a
BWR/6
power
plant
using
RELAP4
MOD5
and
work
with
code
development
personnel
to
improve
the
jet
pump
modeling
and
the
steam
separator
simulation.
The
BWR/6
input
deck
was
developed
using
original
information
from
the
Bingham
Pump
vendor
and
from
General
Electric,
the
power
plant
vendor.
This
model
simulated
the
BWR/6
power
plants
at
River
Bend
Station
and
at
Clinton
Station.
To
supplement
the
heat
transfer
models
of
RELAP4,
FRAP-S
was
used
to
simulate
the
heat
transfer
in
the
8
x
8-fuel
assembly.
This
work
was
performed
for
the
NRC
Research
Staff.
In
addition
to
this
model
development,
several
post
and
pre
test
predictions
were
performed
for
TLTA.
Several
reports
were
written
for
the
NRC
that
described
the
predictions.
Mr.
Miller's
responsibility
was
also
to
monitor
the
testing
at
TLTA,
propose
possible
alternate
testing
and
provide
status
reports
for
the
NRC.
In
addition,
he
helped
develop
scaling
factors
for
the
test
and
provided
part
of
the
testing
plan
for
large
break
LOCA
testing
at
TLTA.
While
at
INEL,
some
technical
support
was
also
given
to
the
early
development
of
RELAP5.
At
Black
&
Veatch
Consulting
Engineers
whom
are
located
in
Overland
Park,
Kansas,
Mr.
Miller
was
responsible
for
all
safety
related
computer
programs
associated
with
thermal
hydraulics.
Black
&
Veatch
was
the
Architecture
Engineer
for
the
Black
Fox
nuclear
power
plant,
which
was
being
built
in
Oklahoma.
Mr.
Miller
was
responsible
for
developing
computer
programs
and
qualifying
them
for
use
on
the
project.
One
example
of
usage
and
code
development
was
in
a
case
where
transient
hydrogen
production
was
simulated
and
released
into
the
containment.
A
version
of
the
MARCH
code
was
modified
and
was
used
to
simulate
the
BWR/6
reactor
vessel
during
a
degraded
core
event.
Tests
were
reviewed
for
hydrogen
production
and
results
were
used
to
validate
the
computer
program.
To
understand
and
respond
to
Utility
and
NRC
questions
on
hydrogen
combustion
and
migration
a
suite
of
computer
programs
was
developed
at
Black
&
Veatch.
This
code
suite
simulated
the
generation,
burning
and
migration
of
hydrogen
in
the
containment.
Mr.
Miller
was
responsible
for
the
development
and
testing
of
this
code
package.
A
program
development
plan
was
written
and
a
validation
plan
was
also
produced.
The
code
package
consisted
of
primarily
two
programs,
HYBRID
and
MIGRAINE.
The
HYBRID
computer
program
used
module
subroutines
from
three
different
programs,
COMPARE,
CONTEMPT
and
MARCH.
HYBRID
could
simulate
pipe
breaks
and
hydrogen
burning
in
subcomparments
and
in
Mark
III
containment/drywell.
It
was
a
finite
difference
lump
mass
computation
that
could
also
track
hydrogen
migration.
MIGRAINE
was
a
more
sophisticated
program,
which
used
SOLA
subroutines
to
track
hydrogen
migration
in
a
three-dimensional
containment
structure.
Black
&
Veatch
participated
in
the
hydrogen
migration-testing
program
conducted
at
EPRI
in
1981.
Black
&
Veatch
provided
pre
test
simulation
results
of
the
hydrogen
migration
test
facility.
A
presentation
of
Black
&
Veatch
results
was
made
at
EPRI
in
San
Jose,
California.
To
develop
the
nuclear
fuel
computer
programs,
an
analysis
and
test
program
plan
was
developed.
Standard
test
problems
such
as
the
Peach
Bottom
Turbine
Trip
tests
were
placed
in
data
banks
for
comparison
to
calculated
results.
Although
the
nuclear
power
plant
was
not
a
test
facility,
much
information
was
obtainable
from
start-up
testing
and
from
the
station
scrams.
This
information
was
retrieved
and
stored
so
comparisons
to
calculated
results
could
be
performed.
For
all
data
stored,
relevant
statistical
uncertainties
were
derived.
The
nuclear
fuel
safety
analysis
test
suite
consisted
of
several
well
know
computer
programs.
These
computer
programs
were
SIMULATE
3,
which
was
used
to
generate
the
three
dimensional
physics
of
the
core,
SIMTRAN,
which
was
used
to
convert
the
3D
physics
to
1D
reactors
kinetics,
ESCORE,
which
was
used
to
provide
the
nuclear
fuel
property
characteristics,
and
RETRAN,
which
used
input
from
SIMTRAN
and
ESCORE
to
simulate
the
reactor
behavior
during
normal
and
abnormal
events.
Simulation
of
the
Peach
Bottom
turbine
trip
using
RETRAN
provided
excellent
agreement
with
the
Peach
Bottom
test
data.
In
addition,
comparison
of
the
results
from
simulated
plant
transients
to
actual
plant
data
provided
good
agreement.
A
topical
Report
was
written
and
presented
to
the
NRC.
In
1984,
Mr.
Miller
was
appointed
Project
Engineer
on
the
pressurizer
safety
valve
qualification
project,
which
was
part
of
NUREG-0737
requirements.
Mr.
Miller
participated,
on
the
Utilities’
behalf,
in
the
safety
valve
testing
at
the
Combustion
Engineering
(CE)
test
facility
in
Windsor,
Connecticut.
Mr.
Miller
provided
reviews
and
comments
on
all
testing
plans
and
witnessed
several
tests
at
the
facility.
As
part
of
his
support
to
the
Utility,
Mr.
Miller
developed
a
RELAP5
model
of
the
pressurizer,
safety
valve
and
discharge
piping.
Modifications
were
made
to
RELAP5
that
included
a
correction
of
the
compressible
gas
subroutine
and
a
correction
to
provide
the
capability
to
calculate
forces
on
the
piping
system.
Comparing
CE
test
results
with
the
RELAP5
calculated
results
were
part
of
the
validation
process.
Mr.
Miller
wrote
a
topical
report
on
the
testing
and
validation
of
the
RELAP5
model
and
submitted
it
to
the
NRC.
All
work
was
found
to
be
acceptable.
Mr.
Miller
was
responsible
for
buying
and
automating
all
the
computers
in
Engineering
Analysis
at
the
RBS.
A
computer
plan
was
developed
and
verification
and
validation
specifications
for
all
software
and
hardware
were
written.
The
plan
consisted
of
developing
a
local
area
network
(LAN)
with
many
PC
as
clients.
Two
RSIC
6000
workstations
were
used
as
servers
and
6
other
RSIC
workstations
along
with
approximately
30
PCs
were
connected
to
the
LAN
clients.
This
arrangement
was
used
to
support
all
Engineering
Analysis
activities
on
site.
back
to
top
Radiation
Protection
and
Criticality
Assessment
Computer
programs,
for
which
Mr.
Miller
prepared
input
decks,
included
ANISN,
DOT
III,
MORSE,
PDQ,
NUMICE
and
KENO.
These
computer
programs
were
used
for
radiation
shielding
and
criticality
simulations.
At
NUS,
Mr.
Miller
was
involved
in
the
design
of
high
density
fuel
racks
for
serveral
different
utilities.
Mr.
Miller
performed
the
following
analyses:
shielding
calculations,
the
minimum
fluid
flow
calculation
through
the
fuel
rack,
the
thermal
hydraulic
departure
from
nucleate
boiling
(DNB)
calculation
for
the
fuel,
the
heat
load
calculation
using
ORIGIN,
and
the
criticality
calculation.
A
report
was
written
for
each
design
and
submitted
to
the
NRC
for
their
review
and
acceptance.
At
River
Bend
Station
(RBS),
several
computer
programs
were
used
to
perform
radiation
transport
calculations.
These
computer
programs
included
ANISN,
CYLDOSE
and
SKYSHINE.
The
off
site
dose
was
calculated
using
a
Stone
&
Webster
computer
program.
Many
analyses
were
provided
for
spent
fuel
shielding
and
radioactive
pipe
shielding.
In
addition,
criticality
of
the
reactor
and
spent
fuel
pool
during
the
fuel
shuffle
was
analyzed.
Aging
analyses
were
also
performed
to
extend
the
life
of
qualified
components.
back
to
top
Engineering
Analysis
In
1985,
Mr.
Miller
accepted
a
position
at
the
River
Bend
Station
working
for
Gulf
States
Utilities.
In
addition
to
several
other
areas
of
responsibility,
Mr.
Miller
was
responsible
for
developing
Engineering
Analysis
at
the
Station.
The
Engineering
Analysis
Group
was
responsible
for
the
following:
the
design
and
specification
of
the
fuel
for
each
reload,
the
development
of
the
probabilistic
safety
assessment
(PSA)
model
for
the
station,
the
development
of
radiation
transport
simulation
and
off-site
dose
calculation
capabilities,
loss
of
coolant
accident
(LOCA)
simulation
and
thermal
hydraulic
simulation
of
the
power
station
reactor
and
systems,
and
the
development
of
a
local
area
network
(LAN)
that
tied
all
the
thermal
hydraulic
and
nuclear
safety
related
computer
programs
and
PCs
to
one
server.
back
to
top
Thermal-Hydraulic
Analyses
A
LOCA
model
of
RBS
was
developed
using
RELAP5
MOD2.
The
LOCA
simulation
results
from
this
model
was
compared
to
General
Electric
calculations
using
SAFER/GESTER
and
good
agreements
between
the
results
of
the
RELAP5
analyses
and
the
results
of
the
SAFER/GESTER
analyses
were
achieved.
Unusual
accident
scenarios
were
also
simulated
using
RELAP5
to
provide
input
into
the
PSA
model.
Other
thermal
hydraulic
models
of
the
reactor
and
associated
systems
were
developed
using
RELAP5
MOD2.
These
models
were
used
to
simulate
many
different
scenarios
that
occurred
or
potentially
could
occur
at
the
plant
so
questions
by
plant
staff
and
oversight
groups
could
be
answered
and
solutions
to
problems
could
be
provided.
Other
thermal
hydraulic
analyses
were
performed
to
determine
the
qualification
of
equipment
under
unusual
circumstances.
Other
computer
programs
used
to
support
these
calculations
were
COMPARE,
CONTAIN,
LOCVS,
GOTHIC
and
CONTEMPT.
To
use
these
programs
efficiently,
an
understanding
of
the
thermal
hydraulic
principals,
theories
and
applications
of
the
computer
programs
was
required.
Additionally,
an
understanding
of
the
reactor,
associated
systems,
and
the
containment
system
was
required.
Most
of
Mr.
Miller's
direct
experience
related
to
a
new
reactor
design
was
in
the
evaluation
of
the
AP600
reactor
design.
In
evaluating
this
design,
Mr.
Miller
was
intimately
familiar
with
the
test
models
at
OSU
and
SPEC-2.
The
test
hardware
and
systems
must
be
evaluated
to
determine
were
abnormal
thermal
hydraulic
behavior
may
occur.
Mr.
Miller
has
developed
these
skills
over
the
years
by
analyzing
many
different
types
of
systems
over
a
spectrum
of
pressures
from
2500
psia
to
0
psia
and
temperatures
that
included
saturated,
subcooled
and
superheated
fluid
conditions.
Mr.
Miller
has
evaluated
heat
transfer
for
pressurized
heat
transfer
surfaces
at
high
velocities
to
natural
circulation
flow
heat
transfer
surfaces
at
low
velocities.
back
to
top
Power
Plant
Support
From
1985
to
1994,
Mr.
Miller
supported
River
Bend
Station
staff
in
resolving
many
different
plant
problems.
He
was
located
on
site
and
the
projects
ranged
from
construction
and
design
to
analysis
and
licensing.
In
1994,
Mr.
Miller
joined
Scientech
as
a
Senior
Technical
Advisor.
His
work
consisted
of
several
projects
for
commercial
utilities
and
the
remaining
tasks
dealt
with
supporting
the
NRC
Research
and
Regulatory
staffs.
In
1996,
Mr.
Miller
started
his
consulting
engineering
firm
and
his
largest
client
was
Commonwealth
Edison
in
Chicago,
Illinois.
Mr.
Miller
began
this
work
with
Commonwealth
Edison
by
evaluating
an
issue
of
the
Auxiliary
Feedwater
Pumps
(AFWPs)
for
Byron
Units
1
&
2
and
Braidwood
Units
1
&
2.
Mr.
Miller
modeled
the
AFW
system
from
the
Condensate
Storage
Tank
(CST)
to
the
Steam
Generators
using
the
computer
program
RELAP5.
With
this
model,
Mr.
Miller
was
able
to
assess
the
root
cause
of
the
problem
and
propose
a
modification.
Once
the
modification
was
implemented,
the
issue
was
resolved.
This
effort
required
him
to
walk
down
the
systems
and
coordinate
information
from
the
site
System
Engineers.
Mr.
Miller
attended
several
meetings
with
plant
staff
to
discuss
results
and
to
evaluate
alternatives.
back
to
top
Quality
Assurance
and
Oversight
Several
projects
were
completed
for
the
NRC.
One
project
consisted
of
performing
a
review
for
the
NRC
staff
on
ASME
code
requirements
of
check
valves
for
PWRs
and
BWRs.
Another
project
consisted
of
reviewing
all
power
uprate
submittals
and
Safety
Evaluation
Reports
and
identifying
technical
areas
that
were
not
adequately
reviewed
and
discussed.
Mr.
Miller
was
also
the
senior
technical
consultant
for
the
NRC
on
two
separate
engineering
inspections
at
nuclear
power
plants.
Reports
were
written
and
presentations
were
made
for
each
of
these
projects.
Mr.
Miller
worked
with
NRC
Research
staff
on
the
review
of
the
APEX
test
facility
at
Oregon
State
University
(OSU)
and
SPES-2
AP600
test
facilities
and
on
the
review
of
Westinghouse
licensing
submittals.
Mr.
Miller
wrote
a
report
comparing
the
RELAP5/MOD3.2
input
decks
of
the
INEL
and
ANSALDO.
Anomalies
between
the
models
and
input
decks
were
noted.
Cases
were
also
run
using
each
of
these
input
decks.
For
another
project,
concerning
the
advanced
reactors,
Mr.
Miller
performed
a
reviewed
of
the
OSU
AP600
test
facility
and
performed
comparisons
of
calculated
results
using
RELAP5/MOD3.2
and
NOTRUMP.
A
report
detailing
the
calculations
of
OSU
test
SB11
was
provided
to
the
NRC
research
staff.
The
APEX
test
SB-11
was
analyzed
using
RELAP5
Mod3.2.
The
APEX
test
facility
at
OSU
was
used
to
simulate
thermal
hydraulic
phenomenon
for
the
AP600
passive
safety
systems
for
loss
of
coolant
accidents
(LOCAs)
and
long
term
cooling.
Another
test,
SB-12,
was
modeled
and
simulated
with
RELAP5
Mod3.2.
The
key
experimental
parameters
measured
were
compared
to
RELAP5
simulation
results.
A
report
was
written
and
the
results
were
presented
to
the
NRC
Research
staff.
back
to
top
Team
Work,
Communication
and
Consensus
Building
At
River
Bend
Station
(RBS)
teamwork
and
consensus
building
was
imperative
to
successfully
managing
the
onsite
Engineering
organization.
Most
work
groups
consisted
of
Maintenance,
Operations,
System
Engineering
and
Engineering
with
oversight
groups
also
participating.
The
oversight
groups
consisted
of
NRC
Inspectors,
Quality
Assurance
and
Control
Staff,
the
Facility
Review
Committee,
and
the
Senior
Oversight
Committee.
All
of
these
groups
had
diverse
backgrounds
and
different
reasons
for
participating
the
projects.
Usually
when
a
significant
problem
occurred,
the
primary
groups,
i.e.,
Operations,
Maintenance,
System
Engineering
and
Engineering
would
hold
a
meeting
to
evaluate
the
problem
and
develop
a
root
cause
for
the
problem.
In
many
cases,
Engineering
would
take
the
lead
and
Mr.
Miller,
as
one
the
lead
engineers,
would
provide
leadership
in
identifying
main
personnel
contributors
for
the
meeting
and
organizing
the
meeting.
Since
most
of
these
groups
had
their
own
"bones
to
pick",
it
was
really
important
to
keep
the
meeting
on
track
and
to
ensure
the
appropriate
individuals
provided
critical
information,
e.g.,
system
performance,
collaborating
test
data
and
analysis,
and
maintenance
and
operation
history.
It
would
generally
take
several
meetings
to
develop
a
satisfactory
root
cause
and
propose
possible
design
changes
to
fix
the
problem.
It
was
always
essential
that
a
consensus
of
the
participants
at
the
meeting
was
reached
and
all
agreed
on
the
root
cause
and
the
corrective
actions
(usually
a
design
modification
along
with
procedures
and
other
document
changes).
The
meeting
notes
were
drawn
up
and
all
participants
concurred
on
the
conclusions
and
recommendations.
Some
of
these
projects
were
very
costly
and
required
more
than
a
year
to
complete
and
it
was
crucial
that
all
major
groups
in
the
company
agreed
with
the
proposed
work
schedule.
Another
example,
in
which
Mr.
Miller
was
involved
in
regulatory
affairs,
occurred
when
Mr.
Miller
was
asked
to
be
the
lead
technical
consultant
for
the
NRC
Engineering
Inspections
at
selected
plant
sites.
This
required
a
meeting
with
NRC
representatives
from
Regions
III
and
IV
at
a
plant
site
and
as
a
team,
perform
an
Engineering
Inspection
of
site
engineering.
The
inspection
team
met
everyday
for
three
weeks
and
discussed
issues
that
surfaced
during
the
day.
Plant
staffs
were
also
involved
in
these
discussions.
It
was
crucial
that
the
team
concurred
on
most
findings,
which
were
presented
to
plant
management
at
the
end
of
the
third
week,
and
later
to
the
NRC
regulatory
staff.
There
were
several
times
that
the
group
disagreed
on
an
issue,
but,
as
a
team,
were
able
to
resolve
them
successfully.
Mr.
Miller,
as
an
engineering
leader
at
River
Bend
Station,
was
responsible
for
plant
operation
24
hours
a
day
and
7
days
a
week.
Many
times,
Mr.
Miller
would
be
called
at
3
A.M.
to
report
to
the
plant
where
a
group
of
people
gathered
to
solve
a
problem
that
could
shut
down
the
plant.
Some
of
these
team
members
did
not
know
each
other
very
well,
but
it
was
necessary
that
these
team
members
worked
together
and
resolve
the
issues.
At
River
Bend
Station,
Mr.
Miller
was
the
emergency
preparedness
Technical
Support
Manager
(TSM)
for
emergency
drills.
This
position
required
excellent
communication
among
all
groups
associated
with
the
drill.
These
groups
included
the
NRC,
civilian
authorities,
company
executives
and
the
staff
in
the
technical
support
center,
included
maintenance,
operations,
systems
engineering
and
design
engineering.
In
these
drills,
decisions
were
quick
and
all
communication
had
to
be
clear
and
succinct.
back
to
top
Testing
and
Oversight
In
1977,
Mr.
Miller
moved
to
Idaho
Falls
to
take
the
position
as
Senior
Engineer
in
Code
Verification
and
Development
at
the
Idaho
National
Engineering
Laboratory
(INEL).
His
immediate
supervisors
were
Tom
Charlton
and
Dick
Rice.
The
laboratory
was
operating
the
Loss
of
Fluid
Test
(LOFT)
facility,
Semi-scale
and
monitoring
the
testing
at
the
Two
Loop
Test
Apparatus
(TLTA)
at
General
Electric
in
San
Jose,
California.
His
first
assignment
was
to
develop
an
input
computer
deck
for
a
BWR/6
using
RELAP4
MOD5
and
work
with
code
development
to
improve
the
jet
pump
modeling
and
the
steam
separator
simulation.
The
BWR/6
input
deck
was
developed
using
original
information
from
the
Bingham
Pump
vendor
and
from
General
Electric
in
San
Jose.
This
model
represented
the
BWR/6
plants
at
River
Bend
Station
and
at
Clinton
Station.
To
supplement
the
heat
transfer
models
of
RELAP4,
FRAP-S
was
used
to
simulate
the
heat
transfer
in
the
8
x
8-fuel
assembly.
This
work
was
performed
for
the
NRC
Research
Staff.
In
addition
to
this
model
development,
several
post
and
pre
test
predictions
were
performed
for
TLTA.
Several
reports
were
written
for
the
NRC
that
described
the
predictions.
Mr.
Miller's
responsibility
was
also
to
monitor
the
testing
at
TLTA
for
the
NRC,
propose
possible
alternate
testing
and
provide
status
reports.
In
addition,
he
helped
develop
scaling
factors
for
the
test
and
provide
part
of
the
testing
plan
for
large
break
LOCA
testing
at
TLTA.
Mr.
Miller
developed
testing
models
and
reviewed
testing
for
Westinghouse's
AP600
test
program.
The
OSU
test
facility
was
used
to
simulate
thermal-hydraulic
phenomenon
for
the
AP600
passive
safety
systems
for
large
and
small
break
loss
of
coolant
accidents
and
long
term
cooling.
During
those
evaluations,
Mr.
Miller
developed
RELAP5
models
that
simulated
the
testing
performed
in
the
APEX
test
facility
at
OSU.
The
OSU
experiments
examined
the
passive
safety
systems
response
for
small
and
large
break
LOCA
transition
into
long
term
cooling.
The
facility
permitted
a
range
of
small-break
LOCAs
to
be
simulated
at
different
locations
on
the
primary
system,
such
as
the
cold
leg
(CL),
hot
leg
(HL),
cold
leg
pressure
balance
line
(PBL),
and
direct
vessel
injection
(DVI)
line.
During
the
thermal
hydraulic
simulation
using
RELAP5,
the
thermal
hydraulic
behavior
of
the
passive
systems
and
the
core
interaction
was
observed.
For
each
of
the
tests,
the
test
data
was
reviewed
for
consistency
and
reasonable
behavior
and
then
the
RELAP5
calculated
results
were
compared
to
the
test
data.
In
many
cases,
there
were
differences
between
the
test
results
and
the
calculated
results.
When
major
differences
occurred,
both
the
experimental
and
the
calculated
results
must
be
reviewed
to
determine
abnormalities.
For
example,
if
the
measured
water
level
in
the
core
was
much
lower
than
the
calculated
water
level,
other
measured
parameters
such
as
inventory
and
mass
balances
were
checked
for
consistency
with
the
water
level
to
ensure
that
the
measurement
was
correct.
For
the
analytical
calculation,
the
inventory
balance
was
also
be
checked
along
with
flow
rates
into
and
out
of
the
reactor
vessel.
For
the
passive,
low
velocity,
and
natural
circulation
code
assessments,
it
was
found
that
in
many
instances,
natural
circulation
and
stratification
were
inherent
in
the
tests.
Since
most
of
the
LOCA
codes
were
based
on
high
velocity
flow,
the
code
assessment
was
focused
on
the
possible
weaknesses
of
the
computer
program
and
new
code
development
was
proposed
to
improve
those
potential
weaknesses.
In
one
project
for
a
commercial
utility,
Mr.
Miller
was
responsible
for
reviewing
the
testing
results
of
a
utility
that
tested
a
proposed
water
level
backfill
modification.
During
their
testing
of
the
modification,
some
anomalies
were
observed
and
the
utility
required
a
review
to
be
performed
of
the
testing
plan,
uncertainties,
scaling
factors
and
test
results
to
determine
if
there
was
a
problem.
A
thorough
review
was
provided
that
also
included
a
RELAP5
model
of
the
test
facility,
which
was
used
to
simulate
the
testing
and
determine
the
root
cause
of
the
anomalies.
It
was
found
from
this
simulation
that
a
small
check
valve
in
the
water
level
instrumentation
line
caused
the
abnormalities
and
that
this
would
not
occur
in
the
actual
design
modification.
On
another
project,
Mr.
Miller
developed
a
safety
valve
dynamic
model
that
was
used
to
evaluate
the
operability
of
the
pressurizer
safety
valves
at
a
PWR
plant.
For
another
project,
Mr.
Miller
was
the
lead
technical
review
engineer
for
the
evaluation
of
three
vendors
that
were
selected
to
perform
small
break
LOCA.
An
inspection
trip
was
taken
to
each
of
the
vendor
locations
and
a
thorough
review
of
their
small
break
LOCA
methods
was
conducted.
This
review
included
the
licensing
of
the
methods,
of
the
method
development,
of
the
testing
that
was
conducted
to
validate
the
programs,
of
the
error
reporting,
and
of
the
unresolved
technical
issues
associated
with
their
computer
programs.
After
these
reviews
were
completed,
a
recommendation
of
a
vendor,
which
met
the
needs
of
the
utility,
was
made
and
a
presentation
was
provided
to
the
utility
board
members.
One
of
the
projects
at
RBS
was
facilitating
the
testing
of
a
critical
component
at
the
station.
A
modification
of
the
control
rod
drive
(CRD)
system
in
the
plant
was
planned
and
a
thorough
test
of
the
changes
was
required
before
the
installation.
During
the
life
of
River
Bend
Station,
cracking
was
observed
in
the
CRD
piping
leading
to
the
CRD
accumulator
tanks.
After
a
reactor
scram,
the
CRD
accumulator
tanks
are
refilled
from
water
taken
from
the
condensate
demineralizer
water
tank
(CDWT).
The
CRD
pumps
took
the
water
from
the
CDWT,
pressurized
the
water
to
1500
psia
and
transported
the
water
through
piping
and
check
valves
into
the
accumulator
tanks.
After
a
number
of
scrams,
it
was
observed
that
the
piping
leading
to
the
accumulator
tanks
was
cracking.
A
root
cause
evaluation
determined
that
the
ball
check
valves
in
the
system
piping
were
chattering
during
refill
and
that
dynamic
vibration
of
the
chattering
ball
check
valves
caused
the
cracking
of
the
associated
pipes.
New
check
valves
were
designed,
but
before
installation,
testing
of
these
valves
in
the
system
was
required.
A
test
plan
and
testing
program
were
developed
that
included
design
drawings,
construction
drawings,
uncertainties,
scaling
factors
and
a
test
matrix.
The
testing
skid
was
constructed
and
testing
was
completed.
Mr.
Miller
has
been
associated
with
some
very
complicated
thermal
hydraulic
problems
that,
in
some
cases,
required
testing
to
resolve.
In
some
of
the
thermal
hydraulic
analytical
work
Mr.
Miller
has
been
involved,
Mr.
Miller
has
successfully
identified
weaknesses
of
the
test
and
of
the
computer
programs
used
to
simulate
the
tests.
Mr.
Miller
has
worked
with
engineers
and
scientists
to
correct
deficiencies
and
Mr.
Miller
has
developed
successful
follow-up
programs
that
lead
to
successful
code
development
and
verification.
back
to
top
Evaluations
of Nuclear Plant Safety Issues
At NUS
Corp. in 1975, Mr. Miller developed models for containment pressurization
and heat-up. He also developed models to simulated reactor
behavior during loss of coolant accidents (LOCAs) and for analyzing
anticipated transient without scram (ATWS) events. These were some of
the initial analyses performed to address ATWS and containment
pressurization concerns.
At
NUS in 1976, Mr. Miller developed safety analysis and licensing submittals
for some of the first high-density fuel rack designs.
Safety analyses were provided for heat generation analyses using
ORIGIN, seismic calculations and criticality analyses.
Thermal hydraulic calculations were performed using basic equations
for natural circulation, parallel flow and DNB correlations.
Licensing submittals were reviewed and approved by the NRC.
At River Bend Station (RBS), the
probabilistic safety analysis (PSA) was used almost daily and Mr. Miller was
the responsible manager and technical lead for its development and use.
Risk assessment was used in fire protection issues, miss-oriented
bundle accidents, stability, HVAC issues, and licensing issues.
An outage risk scenario was developed to help outage planners take
systems out of service with respect to risk.
During several of RBS's outages, risk factors were determined before
the plant was shut down to help planners lay out the outage with respect to
minimizing risk.
A comprehensive safety and risk assessment
enrolled many tools from engineering analysis.
The mechanistic assessment must be conducted to determine the
physical restraints and limitations of the system under investigation. Mechanistic tools used were RELAP5, RETRAN, KYPIPE, NASTRAN
and ADLPIPE. Human factors must
also be factored into the assessment. This
is done through the use of CAFTA using event trees and fault trees.
Sometimes
it is important to determine the probability of a pipe failure just to
determine how credible the event is. Mr.
Miller was the technical lead on many comprehensive safety and risk
assessments using all the elements presented above. Examples are given below.
The power plant was to start-up from an
outage when one of the two main transformers failed.
Since the transformers were not in the Technical Specifications, they
were not considered a safety threat to the plant.
The transformers were not in the PSA model so they were modeled and
included in the PSA model and then risk change probabilities were
determined. Based on the new
evaluation, having one transformer out when the plant started-up was risk
significant and plant staff were informed of the finding.
It was concluded that it was risky to start-up the plant without the
additional transformer. The
plant stayed down for an additional three days so a new transformer could be
installed. This was an
extremely beneficial use of the PSA since it kept plant staff from putting
the plant at risk. This study,
which was performed in 1988, was one of the initial PSA studies that were
used to make a significant safety decision for the plant.
This study helped to provide a benchmark for the nuclear industry,
which began using PSA for non-Technical Specification decision-making.
During
a transient at the plant, high pressure core spray system (HPCS) injection
was initiated. Subsequent to
this event, the motor operated valve (MOV), an isolation valve, was
inadvertently opened when the reactor was at full pressure.
The other isolation valve, which is a check valve, should have closed
against the back flow. Based on
test information taken during the event, it appeared that the check valve
stuck open for a short period of time.
Since this system is designed as a cold-water high-pressure system,
the hot water high-pressure situation represented a potential interfacing
LOCA. Since the MOV was opened
inadvertently and the check valve stuck open for a period of time, it was
necessary to determine how this changed the core damage frequency (CDF) of
the plant. Using mechanistic
methods, it was determined how far the hot water proceeded into the HPCS.
Using this information, a structure analysis was performed to
determine the impact on the structural integrity of the system. This information along with other human factor information
was integrated into the plant PSA to impact on CDF. Since this was a thermal stress cycle to the HPCS that was
not originally factored into the plant PSA, the plant PSA was also changed
to include this condition. This
assessment was significant since it showed plant staff how important it is
to keep check valves in good working order and that an event can change the
CDF of the plant.
At
River Bend Station, Mr. Miller served in several different capacities that
included the development of the ATWS model for boron injection, computer
quality assurance for safety related programs, and the development of
computer codes and programs used to perform engineering analyses on site.
These evaluations were conducted to satisfy parts of the ATWS rule making,
10CFR50.62. Through these evaluations, input for emergency operating
procedures (EOP’s) and design specifications for high-density boron in the
boron injection system were established and implemented.
At
Scientech, Mr. Miller provided senior technical engineering support and
guidance on many technical issues and work assignments that were performed
by in-house staff and by the Nuclear Regulatory Commission’s (NRC’s)
research and regulatory staff. Several reports were written,
which included AP600 testing evaluations, check valve analyses, and an
evaluation of all power uprates performed up to 1996.
On
another project, Mr. Miller developed a safety valve dynamic model that was
used to evaluate the operability of the pressurizer safety valves at a PWR
plant. For another project, Mr. Miller was the lead technical review
engineer for the evaluation of three vendors that were selected to perform
small break LOCA. An inspection trip was taken to each of the vendor
locations and a thorough review of their small break LOCA methods was
conducted. This review included the licensing of the methods, of
the method development, of the testing that was conducted to validate the
programs, of the error reporting, and of the unresolved technical issues
associated with their computer programs. After these reviews were completed,
a recommendation of a vendor, which met the needs of the utility, was made
and a presentation was provided to the utility board members.
Mr.
Miller investigated the effect of water hammer on Fan cooler units (FCUs). FCU are installed in PWRs to cool the containment during
normal operation and, for some designs, to cope with the design-basis
loss-of-coolant accident (LOCA) or main steamline break (MSLB) event
simultaneous with a loss of offsite power (LOOP). The NRC issued GL-96-06,
in part, to address the above concerns. The GL referenced NUREG/CR-5220,
which provides a conservative approach for evaluating waterhammer events.
Loads that were calculated based on EPRI methodology were compared to loads
calculated by RELAP5. The EPRI
methodology includes an analytical model of the closure of an air and steam
pocket, which could cushion the impact of the incoming water slug. The EPRI
model hypothesizes that the pocket contains dissolved air that is released
during boiling, and steam that is left uncondensed before the waterhammer
event occurs. The loads calculated using RELAP5 were slightly more
conservative than the loads calculated using the EPRI methodology.
These loads were used to analyze structural integrity of the FCU
piping for two power plants. A report was issued to the NRC.
back
to
top
Nuclear
Licensing
Mr.
Miller has been involved in many areas of nuclear regulatory oversight and
has given effective communicative presentations and written documentation
for many of the significant issues since 1974.
Mr. Miller is familiar with many NUREGs, Bulletins, Information
Notices, SECY documents, ACRS documents, Generic Safety Issues, Standard
Review Plans, Regulatory Guides, Branch Technical Positions and 10 CFR 50
documents that govern the nuclear industry.
He has addressed most of the major nuclear power plant licensing
issues since the early 1970’s. Some
examples of these issues are provided in the following paragraphs.
At
NUS in 1976, Mr. Miller developed analytical and licensing submittals for
some of the first high-density fuel rack designs.
Licensing submittals were written for 10 fuel rack designs.
RG 1.13, "Spent Fuel Storage Facility Design Basis," and
NUREG-0800, "Standard Review Plan for the Review of Safety Analysis
Reports for Nuclear Power Plants was applied in these evaluations. Quality-assurance
program documents for all rack designed were in compliance with 10 CFR 50,
Appendix B and ANSI N18.2. These
submittals were reviewed and approved by the NRC.
At NUS,
Mr. Miller developed licensing submittals for containment and subcompartment
analyses for the South Texas Project. Original
subcompartment analyses were performed using RELAP3.
RELAP3 was validated against the standard subcompartment problems
provided by the NRC. Mr. Miller
was involved in the first containment fire analysis. These evaluations conformed to Standard Review Plan (SRP)
Chapter 6 (NUREG–0800 and NUREG-75/087), 10CFR50 Appendix B & R and
applicable codes and standards.
In
1983, Mr. Miller provided technical and licensing leadership for the
compliance with 10CFR50.44
"Standards for combustible gas control system in light-water cooled
power reactors”.
Igniter were designed
and located to accommodate the hydrogen generated in the containment and
limit the hydrogen concentration in containment below 10-volume % in
compliance with 10CFR50.34(f) requirements.
Analyses were performed and licensing submittals were provided.
Mr.
Miller developed the technical and licensing submittals for excess hydrogen
management, which included the quantity and location of igniters in a BWR
containment.
On
behalf of a utility client, Mr. Miller was responsible for resolving NUREG
0737 issues with regard to safety and relief valve functionality, TASK
II.D.1 - PERFORMANCE TESTING OF BOILING-WATER REACTOR AND PRESSUREIZER-WATER
REACTOR RELIEF AND SAFETY VALVES (NUREG-0578, SECTION 2.1.2).
Mr. Miller observed testing at the safety valve test facility in
Windsor, Connecticut. He was
responsible for the project that provided the validation of the loop seal
safety valves to function as designed.
He developed a RELAP5 model of the test configurations and compared
results from tests 917 and 908 to calculated results from RELAP5.
He also modeled a safety and relief valve of the power station and
developed loads for ASME Class I piping.